Chris Kouba
Supporter
So I recently purchased an XB3 long block and an Edelbrock EFI to provide the motivation for my car. I'm pretty excited about that and I think it'll be a great combination once it gets going, except something rather bad happened and I'd like to hear from you guys before I hear back from the dealer.
Here's the scoop. I bought the gasket set, the sealers & adhesives, the bolt kit and everything else. I gooped up the surfaces, set the gaskets on them, and rather accurately placed the manifold on them- virtually spot on so no goop squished out.
I started setting in the bolts. I put them all in hand tight and there were no issues. I got the socket set out and snugged them down. Again, no issues. I got the torque wrench out and started to bring them into spec (15-18 ft/lbs). On the bolt between 7 & 8, I got no where near the limit and there was a muffled "pop"- coupled with a lack of resistance turning the bolt and a sinking feeling in my gut
. After I joked to myself that everything seemed to be going to easily and muttering a few words I shouldn't type here:cussing:, I resigned myself to trashing the gasket set to see what just happened with that bolt as it simply felt bad
.
Off with the bolts, off with the manifold, peel back the gaskets and behind door number three is the cast-in boss between intake runners 7 & 8 that had been machined, drilled and tapped but was now in three pieces. It appears that there was some sort of casting flaw in the boss and as the bolt pulled tension on the threads it must have pulled hard enough (seriously- it wasn't that tight) to have it separate.
So why am I airing my dirty laundry for all to read? I am dealing with Anthem Motors outside of Phoenix. They have a call in to FMS to see what they'll do for me. I am soliciting opinions as to what would be an appropriate remedy to the situation. I want to have a thoughtful proposal in case they don't tell me what I want to hear.
I am thinking it'll need a new head. It seems as though it pulled enough of the thread out that I wouldn't want to try to thread into the remaining bore. I am under the assumption that welding up the boss and re-machining could possibly compromise the other machined surfaces and their alignments and I don't want that to be plaguing me for the life of the motor. So it was basically I want a new head (installed) or even just swap them for a new one (long block that is) and they can take care of fixing the other one on their own schedule.
So, are there things I am missing? Options I am overlooking? I don't know how much deeper the threads go so I don't know if a longer bolt is truly an option and the fact that the casting failed in that area already doesn't lead me to want to pursue that option. That was really about the only other one I could think of. Anyone think of anything?
Also, I just wanted to vent without blowing up and I figure someone out there has had something similar happen. Hopefully FMS will do good by me and sort it out. I'm off for a week of climbing now but I am hoping for some good news when I get back though.
Frustratedly,
Chris
Another view
Here's the scoop. I bought the gasket set, the sealers & adhesives, the bolt kit and everything else. I gooped up the surfaces, set the gaskets on them, and rather accurately placed the manifold on them- virtually spot on so no goop squished out.
I started setting in the bolts. I put them all in hand tight and there were no issues. I got the socket set out and snugged them down. Again, no issues. I got the torque wrench out and started to bring them into spec (15-18 ft/lbs). On the bolt between 7 & 8, I got no where near the limit and there was a muffled "pop"- coupled with a lack of resistance turning the bolt and a sinking feeling in my gut


Off with the bolts, off with the manifold, peel back the gaskets and behind door number three is the cast-in boss between intake runners 7 & 8 that had been machined, drilled and tapped but was now in three pieces. It appears that there was some sort of casting flaw in the boss and as the bolt pulled tension on the threads it must have pulled hard enough (seriously- it wasn't that tight) to have it separate.
So why am I airing my dirty laundry for all to read? I am dealing with Anthem Motors outside of Phoenix. They have a call in to FMS to see what they'll do for me. I am soliciting opinions as to what would be an appropriate remedy to the situation. I want to have a thoughtful proposal in case they don't tell me what I want to hear.
I am thinking it'll need a new head. It seems as though it pulled enough of the thread out that I wouldn't want to try to thread into the remaining bore. I am under the assumption that welding up the boss and re-machining could possibly compromise the other machined surfaces and their alignments and I don't want that to be plaguing me for the life of the motor. So it was basically I want a new head (installed) or even just swap them for a new one (long block that is) and they can take care of fixing the other one on their own schedule.
So, are there things I am missing? Options I am overlooking? I don't know how much deeper the threads go so I don't know if a longer bolt is truly an option and the fact that the casting failed in that area already doesn't lead me to want to pursue that option. That was really about the only other one I could think of. Anyone think of anything?
Also, I just wanted to vent without blowing up and I figure someone out there has had something similar happen. Hopefully FMS will do good by me and sort it out. I'm off for a week of climbing now but I am hoping for some good news when I get back though.
Frustratedly,
Chris
Another view
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